I wasn't the only one doing work. Thursday, the aluminum body was made and painted. Friday, we spent time doing the final fittings, drilling hols for the bolts that were outside the designed area, and bolting in the mounting brackets used to connect it to the chassis.
Next, we realized that we didn't have enough time to finish the testing in the lab and we needed to get to the track. So we decided to pack up and head to Stapleford Miniature Railway.
We arrived at 22:00 hours and didn't have a working locomotive. As a whole, we ate some dinner, talked about a plan of attack to make the final connections and apply all the changes. Once we started working we realized another issue with a major component, the tachometer. The tacho was a key feature which was incorporated in every aspect of our design, from cruise control, torque and speed mode switching, applying regenerative braking, etc. We started work on it and found the problem, but at that time, a team around the corner decided to test their air compressed train horn which surprised us while we were soldering a component on the tacho. Needless to say, we couldn't use the tacho anymore. At this point in time we needed to redesign how our locomotive worked. We wen't back to fundamentals, not using the script I had spend dozens of hours on, not using half the circuitry Ivan built, but instead, using the basic features of the motor controller and relying more on the logic circuits built.
After we found out how to utilize the components we had, it was only a matter of time before we were up and running. Six hours later, we had it running. After several more hours of tweaking we had an operational locomotive. It became a fun day of competing.
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